NHTSA Complaint #10020629 — 1991 MITSUBISHI GALANT
ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:EMISSION CONTROL issue reported to NHTSA
Complaint Details
| ODI Number | 10020629 |
| Vehicle | 1991 MITSUBISHI GALANT |
| Component | ENGINE AND ENGINE COOLING:EXHAUST SYSTEM:EMISSION CONTROL |
| Date of Incident | |
| Date Filed | |
| Mileage | 120,090 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | CA |
Consumer Description
I WANT TO FILE A COMPLAIN ABOUT THE ECU FAILURE OF MY 91 MITSUBISHI GALANT. I BOUGHT THIS CAR USED THREE YEARS AGO. RECENTLY, THE CHECK ENGINE LIGHT CAME ON, THE ERROR CODE SHOWED A BAD BAROMETRIC PRESSURE SENSOR. I REPLACED IT AND COULDN'T FIX THE PROBLEM. A SHOP REPLACED IT AGAIN AND THE ERROR CODE WAS STILL THERE. THEY FINALLY DIAGNOZED A BAD ECU. I HAVE HEARD A LOT OF COMPLAINS ABOUT THE EARLY 90S MITSUBISHI GALANT ECU AND HAVE KNOWN AT LEAST TWO OTHER PEOPLE HAVE THE SAME ISSUE. ONE OF MY FRIENDS HAD THE SAME CAR BEFORE, AND THE CAR WAS TOTALLY DEAD ON THE HIGHWAY BECAUSE OF THE ECU FAILURE. FORTUNATELY HE WAS NOT INJURED. HOWEVER, IT'S DEFINITELY A SEVERE ISSUE. I KNOW ANOTHER GUY HAS THE SAME CAR WHEN I AM DOING THE REPAIR. HE HAD A BAD ECU TOO. I AM WONDERING IF YOU HAVE RECEIVED SIMILAR COMPLAINS REGARDING THE ECU.
Related Complaints for the 1991 MITSUBISHI GALANT
Recent Complaints for the 1991 MITSUBISHI GALANT
#10210185
STEERING:LINKAGES:KNUCKLE:SPINDLE:ARM
I HAVE HAD THIS PROBLEM OFF AND ON SINCE 1997 HAVE PUT IN THREE ECM COMPUTERS WHY WAS THIS PROBLEM NEVER ADDRESSED BY...
#10151227
POWER TRAIN:AUTOMATIC TRANSMISSION
TRANSMISSION FAILURE TO SHIFT TO THIRD GEAR AFTER REPLACING TRANSMISSION WITH OTHER UNIT LESS THAN A YEAR AGO. ( APRI...
#10070668
EQUIPMENT:ELECTRICAL
RIGHT BOOT HAS SELF DESTRUCTED FOR THE THIRD TIME (THE FIRST TIME WAS AROUND 35000 & I WAS TOLD THEY SHOULD BE GOOD F...
#10070552
POWER TRAIN
PURCHASED A VEHICLE AT EASTABOGA AUTO SALES. DROVE THE CAR FOR 1 DAY THE TRANSMISSION STARTED ACTING UP I TOOK IT BAC...
#10070668
POWER TRAIN
RIGHT BOOT HAS SELF DESTRUCTED FOR THE THIRD TIME (THE FIRST TIME WAS AROUND 35000 & I WAS TOLD THEY SHOULD BE GOOD F...