NHTSA Complaint #10186776 — 1997 FORD F-150
ENGINE AND ENGINE COOLING issue reported to NHTSA
Complaint Details
| ODI Number | 10186776 |
| Vehicle | 1997 FORD F-150 |
| Component | ENGINE AND ENGINE COOLING |
| Date of Incident | |
| Date Filed | |
| Mileage | 47,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | NY |
Consumer Description
I JUST GOT MY 1997 FORD F150 XLT WITH THE 4.2L ENGINE BACK YESTERDAY, AFTER PAYING $1430 FOR ENGINE REPAIRS. THIS TRUCK ONLY HAS 47,700 MILES ON IT. I WENT OUT TO THE TRUCK ONE DAY AND TURNED THE KEY, AND - NOTHING. TURNS OUT TO BE HYDRO LOCK BUT I DIDN'T KNOW IT AT THE TIME. I FINALLY GOT IT STARTED, & GOT IT INTO THE DEALER, AND THE TECHNICIAN THOUGHT IT NEEDED TO BE TUNED UP, PLUS I WAS HAVING THE HEAT FADE AT STOPS SO HE FLUSHED & REFILLED THE COOLANT. I MENTIONED THAT I WAS HAVING TO TOP OFF THE COOLANT ABOUT ONCE A MONTH, BUT I DIDN'T KNOW WHERE THE COOLANT WAS GOING, AND IT WASN'T SHOWING UP IN THE OIL. I GOT IT BACK, AND IT WAS STILL RUNNING REALLY BAD, SO I DROPPED IT OFF AGAIN 2 DAYS LATER. THIS TIME HE THOUGHT IT WAS THE COIL PACK. THEY HAD IT AGAIN FOR ANOTHER DAY, REPLACED THE COIL PACK AND A SENSOR. I GO OUT TO THE LOT AND START IT, AND IT WAS STILL RUNNING REALLY BAD. SO, I GO BACK IN & GET THE TECHNICIAN, AND HE CAME OUT TO CHECK IT HIMSELF, AND HE WAS AMAZED AT HOW BAD IT WAS RUNNING. WE TOOK IT FOR A RIDE, AND IT SMOOTHED OUT A LITTLE, BUT IT WAS STILL NOT RIGHT. I TOLD HIM I WOULD LET HIM CONSULT HIS BOSS, AND CALL THEM BACK ON MONDAY. MONDAY COMES, AND I GO TO START IT TO GO TO WORK, AND - HYDRO LOCK AGAIN. SO, I TAKE MY WIFE'S CAR TO WORK, AND CALLED THEM FROM THERE, AND TOLD THEM WHAT IT WAS DOING. THEY WERE THERE WITHIN A HALF HOUR TO GET IT. THIS TIME I GET A CALL FROM THE SERVICE MANAGER, AND HE TOLD ME THAT HE PUT HIS BEST TECHNICIAN ON IT, AND WOULD CALL. WHEN HE CALLED, HE TOLD ME THAT THE HEAD GASKETS WERE LEAKING, AND LETTING COOLANT INTO THE CYLINDERS. I SAID TO GO AHEAD & FIX IT. THEN THEY CALLED ME BACK THE NEXT DAY AND TOLD ME THAT THEY FOUND THAT THE LOWER INTAKE MANIFOLD WAS CRACKED, AND LETTING COOLANT POUR INTO THE CYLINDERS. I ASKED ABOUT GETTING A USED INTAKE MANIFOLD, AND HE SAID THEY WOULD LOOK FOR ONE, AND THEY DID FIND ONE. PLUS, THEY PUT IN A NEW THERMOSTAT. *JB
Related Complaints for the 1997 FORD F-150
Other ENGINE AND ENGINE COOLING Complaints
#10457670
FORD RECALL 99B29. FRONT COVER GASK UNABLE TO HOLD COOLANT. *TR
#10455460
TRUCK HAS A 4.2 LITER, V-6 ENGINE. A WEEK PRIOR TO INCIDENT THE TRUCK WAS DRIVEN THEN PARKED IN A MY GARAGE. ON TH...
#10453097
TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT AFTER PARKING THE VEHICLE, HE HEARD THE HORN SOUNDING...
#10452801
TL* THE CONTACT OWNS 1997 FORD F-150. THE CONTACT STATED THAT AFTER RECEIVING NOTIFICATION OF NHTSA CAMPAIGN I.D. 11V...
#10451937
TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT THE VEHICLE CAUGHT ON FIRE WHILE PARKED. NO ONE WAS I...
Recent Complaints for the 1997 FORD F-150
#11582405
POWER TRAIN
The contact owns a 1997 Ford F-150. The contact stated that while driving at undisclosed speeds, the transmission hes...
#11552635
SERVICE BRAKES
on two occasions now while traversing a slight downgrade (approx 8-10mph) applied brake (per pedal) and vehicle fail...
#11541608
POWER TRAIN
The contact owns a 1997 Ford F-150. The contact stated that while attempting to park the vehicle, the vehicle failed ...
#11517479
SERVICE BRAKES
1997 Ford F150, had recall 25527072 05S28 performed in March of 2006. The switch installed as part of the recall has...
#11517479
VEHICLE SPEED CONTROL
1997 Ford F150, had recall 25527072 05S28 performed in March of 2006. The switch installed as part of the recall has...