NHTSA Complaint #10135752 — 1993 FORD MUSTANG
VEHICLE SPEED CONTROL:LINKAGES issue reported to NHTSA
Complaint Details
| ODI Number | 10135752 |
| Vehicle | 1993 FORD MUSTANG |
| Component | VEHICLE SPEED CONTROL:LINKAGES |
| Date of Incident | |
| Date Filed | |
| Mileage | 82,000 miles |
| Crash | No |
| Fire | No |
| Injuries | 0 |
| Deaths | 0 |
| Vehicle Towed | No |
| State | VA |
Consumer Description
STUCK GAS PEDAL THROTTLE LINKAGE CAUSING CONTINUOUS FULL THROTTLE TRANSMISSION KICK DOWN CABLE ON 1993 FORD MUSTANG 5.0 LX MUSTANG THAT CONTROLS FLUID DELIVERY TO TRANSMISSION OVERDRIVE AND IS ATTACHED TO THROTTLE CONTROLS BY A GROMMET CAME OFF AT HIGHWAY SPEEDS. THE GROMMET FAILED PROBABLY DUE TO AGE, AND THE TRANSMISSION DESTROYS THE OVERDRIVE PORTION OF ITS SELF LEAVING THE DRIVER ONLY ABLE TO GO APPROXIMATELY 45 MPH IN OVERDRIVE POSITION AND ANYTHING OVER THE SHIFTING SPEED INTO OVERDRIVE JUST LETS THE ENGINE RPM RUN AWAY AND THE TRANSMISSION TO SLIP. THE REAL PROBLEM THEN OCCURS IF THE DRIVER USES THE DRIVE POSITION TO GET THE VEHICLE BACK TO HIGHWAY SPEEDS AND NO SLIPPING OF THE TRANSMISSION. IF THE ACCELERATOR IS PUSHED CLOSE TO THE FLOOR, IT ALLOWS THE NOW FLOATING FREE KICK DOWN CABLE TO JAM THE THROTTLE TO FULL OPEN CAUSING A STUCK ACCELERATOR AND THE ONLY WAY TO FREE IT IS TO GET TO NEUTRAL QUICKLY AND TURN OFF IGNITION SWITCH, THEN UNJAM THE CABLE AND THROTTLE LINKAGE BY HAND. POSSIBLE ACCIDENTS/INJURIES OR DEATHS COULD RESULT, ESPECIALLY WHEN IT HAPPENS FROM A STANDING STOP AT AN INTERSECTION, OR IN MY CASE, A HOUSING 25 MPH RESIDENTIAL ZONE. THE TRANSMISSION HAS TO BE REBUILT AND THE GROMMET KICK DOWN CABLE GROMMET REPLACED. THE OLD GROMMET ON MY VEHICLE IS NO LONGER AVAILABLE. THE CABLE AND GROMMET SHOULD BE ON SOME TYPE OF INSPECTION OR REPLACEMENT SCHEDULE/OR REDESIGNED TO KEEP THIS FROM HAPPENING. I HAVE SEEN TWO OTHER MUSTANGS WITH THE SAME PROBLEM I HAD WITH ONE OF THE VEHICLES BEING DRIVEN BY A YOUNG FEMALE WHO PULLED THE VEHICLE IN TO MY WORK AREA(LOT) WITH A RUN AWAY ENGINE IE STUCK GAS PEDAL. I UNSTUCK HER KICKDOWN CABLE AND GAVE HER ADVICE ON REPAIRS AND WHAT WAS WRONG AND COULD HAPPEN.*JB
Related Complaints for the 1993 FORD MUSTANG
Recent Complaints for the 1993 FORD MUSTANG
#10664922
AIR BAGS
MY NAME IS [XXX] AS [XXX] I WAS IN AN ACCIDENT IN 1997 WHILE DRIVING MY SON IN LAWS FORD MUSTANG THE AIRBAG DEPLOYED ...
#10218969
ELECTRICAL SYSTEM
I BOUGHT A 93 MUSTANG 4 CYLINDER WITH 12,000 MILES ON IT IN 12\93. THE CAR NOW ONLY HAS 28,000 MILES ON IT TOTAL. T...
#10218969
LATCHES/LOCKS/LINKAGES
I BOUGHT A 93 MUSTANG 4 CYLINDER WITH 12,000 MILES ON IT IN 12\93. THE CAR NOW ONLY HAS 28,000 MILES ON IT TOTAL. T...
#10218969
STRUCTURE
I BOUGHT A 93 MUSTANG 4 CYLINDER WITH 12,000 MILES ON IT IN 12\93. THE CAR NOW ONLY HAS 28,000 MILES ON IT TOTAL. T...
#10166251
ELECTRICAL SYSTEM:IGNITION
1993 FORD MUSTANG IGNITION SYSTEM FIRE VEHICLE WAS IN GARAGE AFTER BEING DRIVEN THE DAY BEFORE. ATTEMPTED TO START ...